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Daqing Petrochemical Refinery's Lubricating White Clay Unit has been using activated clay as a refined additive to remove non-ideal components in lubricating oil and improve the color and stability of lubricating oil. Although it is possible to meet the quality requirements for lubricating oil components, the energy consumption of the device is high, and the large amount of waste generated is an environmental problem. In order to optimize the use of "three agents" and reduce processing costs, the plant has compared and applied dozens of additives. It was found that the BLS-X100 adsorbent of Hubei Jinhe Chemical Co., Ltd. has the effect of replacing activated clay, and the reconciled lubrication The oil component oil is of excellent quality.
Afterwards, the plant listed the application of lube oil plants as a key technical reform project of this year, and implemented technological transformations to the feeding system of the powder feeder, the mixing tank mixing system and the steam heating system, and used the BLS-X100 type cryogenic adsorbent instead. White clay is refined with lubricating base oil. The application effect of the adsorbent is exactly the same as the original process, and it is a low-temperature and high-efficiency adsorbent. The heating process of the heating furnace can be eliminated during the production process. It is estimated that 1800 tons of fuel gas can be saved per year, and the energy consumption of the device can be reduced by 70%. The annual increase in benefit is 1.8 million yuan. In addition, the amount of new adsorbent added is only 1/10 of the amount of white clay added, which can not only increase the refined oil yield, but also extend the life cycle of filter paper and filter cloth, and can save the cost of 2.28 million yuan annually.
Daqing Petrochemical Refinery's low-temperature lubricant adsorption device has been successfully fed once and produced qualified products. After the implementation of the Lubricant Plant application of non-blanket technology transformation project, the plant energy consumption can be reduced by 70%, the production cost can be reduced by 4 million yuan.